Actions for Innovative Clean Coal Technology (ICCT) [electronic resource] : 500 MW demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NO{sub x}) emissions from coal-fired boilers. Third quarterly technical progress report
Innovative Clean Coal Technology (ICCT) [electronic resource] : 500 MW demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NO{sub x}) emissions from coal-fired boilers. Third quarterly technical progress report
- Published
- Washington, D.C. : United States. Dept. of Energy, 1993.
Oak Ridge, Tenn. : Distributed by the Office of Scientific and Technical Information, U.S. Dept. of Energy. - Physical Description
- 72 pages : digital, PDF file
- Additional Creators
- United States. Department of Energy and United States. Department of Energy. Office of Scientific and Technical Information
Access Online
- Restrictions on Access
- Free-to-read Unrestricted online access
- Summary
- This quarterly report discusses the technical progress of an Innovative Clean Coal Technology (ICCT) demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NOₓ) emissions from coal-fired boilers. The project provides a stepwise retrofit of an advanced overfire air (AOFA) system followed by low NOₓ burners (LNB). During each test phase of the project, diagnostic, performance, long-term, and verification testing will be performed. These tests are used to quantify the NOₓ reductions of each technology and evaluate the effects of those reductions on other combustion parameters such as particulate characteristics and boiler efficiency. Baseline, AOFA, LNB, and LNB plus AOFA test segments have been completed. Analysis of the 94 days of LNB long-term data collected show the full-load NOₓ emission levels to be approximately 0.65 lb/MBtu with fly ash LOI values of approximately 8 percent. Corresponding values for the AOFA configuration are 0.94 lb/MBtu and approximately 10 percent. For comparison, the long-term full-load, baseline NOₓ emission level was approximately 1.24 lb/MBtu at 5.2 percent LOI. Comprehensive testing in the LNB+AOFA configuration indicate that at full-load, NOₓ emissions and fly ash LOI are near 0.40 lb/MBtu and 8 percent, respectively. However, it is believed that a substantial portion of the incremental change in NOₓ emissions between the LNB and LNB+AOFA configurations is the result of additional burner tuning and other operational adjustments and is not the result of the AOFA system. During this quarter, LNB+AOFA testing was concluded. Testing performed during this quarter included long-term and verification testing in the LNB+AOFA configuration.
- Report Numbers
- E 1.99:doe/pc/89651--t13
doe/pc/89651--t13 - Subject(s)
- Other Subject(s)
- Note
- Published through SciTech Connect.
12/31/1993.
"doe/pc/89651--t13"
"DE94014337"
"AZ0404010"
Not Available.
Southern Co. Services, Inc., Birmingham, AL (United States) - Type of Report and Period Covered Note
- Quarterly; 07/01/1993 - 09/30/1993
- Funding Information
- FC22-90PC89651
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