Actions for Formation plugging while testing a steam well at The Geysers [electronic resource].
Formation plugging while testing a steam well at The Geysers [electronic resource].
- Published
- Washington, D.C. : United States. Dept. of Energy, 1978.
Oak Ridge, Tenn. : Distributed by the Office of Scientific and Technical Information, U.S. Dept. of Energy. - Physical Description
- pages 106-111 : digital, PDF file
- Additional Creators
- United States. Department of Energy and United States. Department of Energy. Office of Scientific and Technical Information
Access Online
- Restrictions on Access
- Free-to-read Unrestricted online access
- Summary
- During testing of a steam well at The Geysers steam field in Sonoma County, California, rate suddenly dropped by 17,500 lb/hr and wellhead pressure simultaneously increased by 30 psi. There was no evidence of plugging in any of the surface facilities downstream of the wellhead. Pressure buildup tests before and after the incident show that there was a 15% reduction in permeability-thickness. Analysis of pressure losses in the wellbore due to friction showed that all of the rise in wellhead pressure could be explained by the reduction in mass flow that occurred as a result of the 15% reduction in kh. The change in wellhead enthalpy from 1200 Btu/lb and 4-5 F superheat prior to the incident to 1197 Btu/lb and 0-1.4 F superheat after the incident indicates the well became slightly wet. One possible explanation for this reduction in kh is that movement of free water caused a plugging action or a reduction of mobility to steam in one or more steam entries.
- Report Numbers
- E 1.99:sgp-tr-30
E 1.99: conf-781222-14
conf-781222-14
sgp-tr-30 - Subject(s)
- Other Subject(s)
- Note
- Published through SciTech Connect.
01/01/1978.
"sgp-tr-30"
" conf-781222-14"
Proceedings fourth workshop geothermal reservoir engineering, Stanford, CA, December 13-15, 1978.
Strobel, Calvin J.
Union Oil Company of California, Santa Rosa, CA
View MARC record | catkey: 14384817