Space Shuttle Main Propulsion System Gaseous Hydrogen Flow Control Valve Poppet Failure
- Author:
- Zeitler, Rick
- Published:
- May 10, 2010.
- Physical Description:
- 1 electronic document
Online Version
- hdl.handle.net , Connect to this object online.
- Restrictions on Access:
- Unclassified, Unlimited, Publicly available.
Free-to-read Unrestricted online access - Summary:
- The presentation provides background information pertinent to the MPS GH2 Flow Control Valve Poppet failure which occurred on the Space Shuttle Endeavour during STS-126 flight. The presentation provides general MPS system operating information which is pertinent to understanding the failure causes and affects. The presentation provides additional background information on the operating environment in which the FCV functions and basic design history of the flow control valve. The presentation provides an overview of the possible flight failure modes and a brief summary of the flight rationale which was developed for this failure event. This presentation is an introductory presentation to 3 other speakers at the conference who will be speaking on M&P aspects of the investigation, non destructive inspection techniques development, and particle impact testing.
- Other Subject(s):
- Collection:
- NASA Technical Reports Server (NTRS) Collection.
- Note:
- Document ID: 20110003995.
KSC-2010-056.
2010 Aircraft Airworthiness and Sustainment Conference; 10-13 May 2010; Austin, TX; United States. - Terms of Use and Reproduction:
- Copyright, Distribution under U.S. Government purpose rights.
View MARC record | catkey: 15992784